I'll try that, but the volume of fluid that came out made me think it was more than a crack. I think its drilled too deep. I don't know if my header bolts vs. the original manifold studs could have contributed. My machinist did do some extra work on the head as a different bolt hole had been drilled crooked for an easy out and had half a bolt "keyed" into the head with half an easy out. He then ran a tap through the the rest of the holes to make sure the threads were solid
Will the locktite sealant make it difficult to get the bolt out next time? I don't plan on taking the headers off in the near future, but I seem to be good at twisting bolts off.
1984 F250 4x4 351W ZF5-42