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Yes, I'm guessing that whomever installed the balancer last just barely got the bolt started and tried to torque it to get the balancer to go in. Maybe it was cross-threaded or the balancer was cocked and didn't want to go in, but that pulled the first bit of the thread off the crank.
But I don't think that is going to be a problem at all.
Gary, AKA "Gary fellow": Profile
Dad's: '81 F150 Ranger XLT 4x4: Down for restomod: Full-roller "stroked 351M" w/Trick Flow heads & intake, EEC-V SEFI/E4OD/3.50 gears w/Kevlar clutches
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In reply to this post by ArdWrknTrk
First half thread and no impact wrench on my part. I used a rented puller and installer and a lot of elbow grease. It did take a lot of effort to get the old balancer moving but once it started it came off pretty easy.
Will
-- 1982 F-250 HD 4x4 400/C6 4.10 Dana61 (Borgeson/Bluetop/Lee, 3G) |
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They can get stuck pretty good.
I only asked about using an impact because I know how threads behave in steel and cast iron. I agree with Gary. There's no issue with the crank losing that little chip but I wouldn't use thread locker on the bolt.
Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake. Too much other stuff to mention. |
In reply to this post by Gary Lewis
I gave up on pulling the fuel pump to check the timing chain. I was getting prepared to do that next but it looked like I might need to remove the fuel lines to get the pump off and far enough out of the way. I was close to giving up on checking the chain altogether. Last night I stumbled onto a video showing the same distributor process you described previously. For some reason, when I first read your description, it sounded much more difficult.
So, going the distributor and rotor route, I could not find any difference in movement. My spring loaded TDC tool arrived since I started all of this work and it made finding TDC a breeze. After getting there, I pulled the cap and found that I was on the exhaust stroke. I rotated the engine around to the compression stroke and followed the rotor the entire way around. I could not see any difference in the movement. Once at the correct TDC, I slowly moved back and forth from there and the rotor moved immediately both directions. I honestly could not find any different in the movement. If there is any, it is very minimal, probably less than a degree. Tomorrow, I plan to start cleaning up some of the exposed bits and then start putting everything else back on. Oh, and the balancer markings. TDC is not at 0 on the balancer. No more -7 degrees like the old balancer. Also, I checked it again before removing the old balancer and we were still at -7 degrees.
Will
-- 1982 F-250 HD 4x4 400/C6 4.10 Dana61 (Borgeson/Bluetop/Lee, 3G) |
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That being the case then you don't need to replacing the timing chain.
But I'm not sure I understand where the point is vs TDC on the new balancer. I think you said it is -7 degrees on the old balancer, but I got lost with what you were saying about the new one.
Gary, AKA "Gary fellow": Profile
Dad's: '81 F150 Ranger XLT 4x4: Down for restomod: Full-roller "stroked 351M" w/Trick Flow heads & intake, EEC-V SEFI/E4OD/3.50 gears w/Kevlar clutches
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Gary, It's been a long week!
At TDC, the old balancer was showing 7 degrees off from 0. So it had definitely slipped and wasn't just separating.
Will
-- 1982 F-250 HD 4x4 400/C6 4.10 Dana61 (Borgeson/Bluetop/Lee, 3G) |
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In reply to this post by dirtymac
I went back to the beginning and read what you have to say. 1st, I have to ask when setting the base timing do you have the distributor disconnected and the vacuum line plugged? 22° should have the starter struggling to turn the engine and kicking back when you release the key. A DS-II ignition module should retard the ignition timing a few degrees while the starter is engaged, but not more than 4° or so. (I think Gary measured it in milliseconds with his O-scope) Reconnect the vacuum line and I'd expect 22° to be a minimum for proper timing at idle. But this still doesn't explain your suggestion that "The factory setting was 3° of timing" It should say on.the emissions sticker to set the timing at 8° with the curb idle set to something like 650 in drive for automatics. Also, never use Teflon tape on fuel fittings. The previous owner must not understand that fuel systems rely on flare fittings, which seal metal on metal. The nut only applies pressure to hold the flare together. If fuel has reached the threads the flared line and filter are not doing their primary job. Given that you observe a bunch of excess silicone glopped around the timing case (cover plate, In a 335 series engine?) I'd expect the chain and sprockets were changed not too many miles ago. There's nothing else in there, for it to have been removed. When trying to determine if the harmonic damper's timing ring has slipped it shouldn't really matter whether you are on compression or exhaust. The damper is keyed directly to the crank. The pistons go up and down with the crank as well. It's only the cam that turns at 1/2 speed (because the cam gear has twice as many teeth as the crank gear)
Jim,
Lil'Red is a '87 F250 HD, 4.10's, 1356 4x4, Zf-5, 3G, PMGR, Saginaw PS, desmogged with a Holley 80508 and Performer intake. Too much other stuff to mention. |
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